Violation Detail
Standard Cited: 19100119 F01 II A Process safety management of highly hazardous chemicals.
Inspection Nr: 1524024.015
Citation: 01016
Citation Type: Serious
Abatement Date: 11/12/2021
Initial Penalty: $13,653.00
Current Penalty: $13,653.00
Issuance Date: 10/06/2021
Nr Instances: 5
Nr Exposed: 68
Related Event Code (REC): A;R
Gravity: 10
Report ID: 0522500
Contest Date: 10/25/2021
Final Order:
Emphasis:
Type | Latest Event | Event Date | Penalty | Abatement Due Date | Citation Type | Failure to Abate Inspection |
---|---|---|---|---|---|---|
Penalty | C: Contested | 10/29/2021 | $13,653.00 | 11/12/2021 | Serious | |
Penalty | Z: Issued | 10/06/2021 | $13,653.00 | 11/12/2021 | Serious |
Text For Citation: 01 Item/Group: 016 Hazard:
29 CFR 1910.119(f)(1): Operating procedures. The employer did not develop and implement written operating procedures that provide clear instructions for safely conducting activities involved in each covered process consistent with the process safety information and shall address at least the following elements. 29 CFR 1910.119(f)(1)(ii): Operating limits: 29 CFR 1910.119(f)(1)(ii)(A):Consequences of deviation; a. On or about and prior to April 8, 2021, the written operating procedure, K3, K4, K5 Agitator Operation, RES-PRO-KO-007, failed to address the loss of cooling water and the loss of agitation during agitator use in covered process operations. On April 8, 2021, the kettle 3 reactor vessel manway failed and released vapor into the kettle 3/kettle 4 room. Just prior to the vapor release, agitation loss was discovered and was restored to operation at normal speed. This catastrophic failure resulted in the explosion event that resulted in a fatality and multiple disabling injuries. b. On or about and prior to April 8, 2021, the written operating procedure, Kettle 3 Overhead Processing Procedure, RES-PRO-022, failed to address the disruption of flow (or blockage of equipment) in the overhead system, failed to address the return of water into the reactor vessel that can result in "foaming," failed to address the loss of cooling water and failed to address the loss of agitation during agitator use in the reactor vessel. On April 8, 2021, the kettle 3 reactor vessel manway failed and released vapor into the kettle 3/kettle 4 room. Just prior to the vapor release, agitation loss was discovered and was restored to operation at normal speed. This catastrophic failure resulted in the explosion event that resulted in a fatality and multiple disabling injuries. c. On or about and prior to April 8, 2021, the written operating procedure, Solvent Manifold Operation, RES-PRO-PLT-031, failed to address the disruption of flow (or blockage of equipment) in the overhead system, failed to address the return of water into the reactor vessel that can result in "foaming," failed to address the loss of cooling water and failed to address the loss of agitation during agitator use in high temperature reactor vessels in covered process operations. On April 8, 2021, the kettle 3 reactor vessel manway failed and released vapor into the kettle 3/kettle 4 room. Just prior to the vapor release, agitation loss was discovered and was restored to operation at normal speed. This catastrophic failure resulted in the explosion event that resulted in a fatality and multiple disabling injuries. d. On or about and prior to April 8, 2021, the written operating procedure, K3 and K4 Eductor Operation, RES-PRO-KO-005, failed to address the disruption of flow (or blockage of equipment) in the overhead system, failed to address the return of water into the reactor vessel that can result in "foaming," failed to address the loss of cooling water and failed to address the loss of agitation during agitator use in high temperature reactor vessels in covered process operations. On April 8, 2021, the kettle 3 reactor vessel manway failed and released vapor into the kettle 3/kettle 4 room. Just prior to the vapor release, agitation loss was discovered and was restored to operation at normal speed. This catastrophic failure resulted in the explosion event that resulted in a fatality and multiple disabling injuries. e. On or about and prior to April 8, 2021, the written operating procedure, OPC Emergency Shutdown Procedure, RES-PRO-PLT-009, failed to address the loss of cooling water and the loss of agitation during agitator use in covered process operations. On April 8, 2021, the kettle 3 reactor vessel manway failed and released vapor into the kettle 3/kettle 4 room. Just prior to the vapor release, agitation loss was discovered and was restored to operation at normal speed. This catastrophic failure resulted in the explosion event that resulted in a fatality and multiple disabling injuries.