Violation Detail
Standard Cited: 19100119 D03 I B Process safety management of highly hazardous chemicals.
This violation item has been deleted.
Inspection Nr: 1570275.015
Citation: 02001
Citation Type: Other
Abatement Date: 07/22/2022
Initial Penalty: $1,163.00
Current Penalty: $0.00
Issuance Date: 06/03/2022
Nr Instances: 3
Nr Exposed: 10
Related Event Code (REC): R
Gravity:
Report ID: 0626600
Contest Date:
Final Order: 07/15/2022
Emphasis:
Type | Latest Event | Event Date | Penalty | Abatement Due Date | Citation Type | Failure to Abate Inspection |
---|---|---|---|---|---|---|
Penalty | I: Informal Settlement | 07/15/2022 | $0.00 | 07/22/2022 | Other | |
Penalty | Z: Issued | 06/03/2022 | $1,163.00 | 07/22/2022 | Other |
Text For Citation: 02 Item/Group: 001 Hazard:
29 CFR 1910.119(d)(3)(i)(B): Process Safety Information pertaining to the piping and instrumentation diagrams (P&ID) was not compiled, complete and accurate. This violation was most recently observed on or about December 23, 2021, in Hydro Desulfurization Unit (HDU-1) at ExxonMobil refinery located in Baytown, TX, when the employer did not ensure Process Safety Information (PSI) such as Piping and Instrumentation Diagram (P&ID) # 134-500-0058, Rev 4, was complete and accurate included, but not limited to the following: a. 14-inch flanges were missing on a bypass line from furnace F-701 to reactor R-702B. b. Line number 0-084-14"-300# was missing for 14-inch bypass line. c. Normally closed (NC) symbols were missing for valves ROV-075 and ROV-605.